Club Cobra Gas-N Exhaust  

Go Back   Club Cobra > Club Forums > Bowtie Snakes

MMG Superformance
Nevada Classics
Main Menu
Module Jump:
Nevada Classics
Nevada Classics
MMG Superformance
MMG Superformance
Advertise at CC
Banner Ad Rates
MMG Superformance
Keith Craft Racing
MMG Superformance
Keith Craft Racing
May 2026
S M T W T F S
          1 2
3 4 5 6 7 8 9
10 11 12 13 14 15 16
17 18 19 20 21 22 23
24 25 26 27 28 29 30
31            

Kirkham Motorsports

 
 
LinkBack Thread Tools Display Modes
Prev Previous Post   Next Post Next
  #11 (permalink)  
Old 02-26-2002, 01:49 AM
CC Member
Visit my Photo Gallery

 
Join Date: Nov 2001
Posts: 7
Not Ranked     
Default

Jeff thanks for the suggestion, and you were right, There was a problem with the ignition and advance.

I took ages trying to sort this problem, and after a problem with a noisy pilot bearing on the end of the gearbox shaft, eventually pulled the block (I needed to for the bearing) and took the block along to the engine dyno guy. along with all the movable electic paraphanalia, fuel bits etc. First thing was a base line run, which showed the block running very rich, then leaning out at the top end, first thing he did was rip off the fuel regulator & fitted a replacement, then fitted lighter springs to the holley vac secs, which sorted variance, then on to the ignition, which he set by dwell angle, and vac advance, which was set up at 43 degrees, but there was a lot of discussion here as it was set back to 40 and lost power. we eventually decided that the pointer may not be accurate as TDC, cam alignment etc were all spot on.
The advance was also coming on too aggressively, and this was adjusted with a allen key in the vac chamber. We eventually got 390 hp, 440 torque.

Then we put on the headers supplied with the kit, pulled again, and lost 6 hp over the dyno optimised headers, which was considered OK as my headers did not have a collector (the collector is on the muffler)and may not scavenge properly. we then added sidepipes and lost 30hp. the problem here was we couldn't vent these through the dyno exhaust, and the dyno guy felt that the exhaust was recirculating within the dyno chamber, and reducing the o2 available, causing the drop in performance.

I am not sure at the moment if I have a problem here or not, but the block is running good numbers, not leaning or running rich, I guess I'll have to wait till I get it back together before I know
Reply With Quote
 


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off
Trackbacks are On
Pingbacks are On
Refbacks are On



All times are GMT -7. The time now is 03:07 AM.


Powered by vBulletin® Version 3.8.0
Copyright ©2000 - 2026, Jelsoft Enterprises Ltd.
Search Engine Friendly URLs by vBSEO 3.6.0
The representations expressed are the representations and opinions of the clubcobra.com forum members and do not necessarily reflect the opinions and viewpoints of the site owners, moderators, Shelby American, any other replica manufacturer, Ford Motor Company. This website has been planned and developed by clubcobra.com and its forum members and should not be construed as being endorsed by Ford Motor Company, or Shelby American or any other manufacturer unless expressly noted by that entity. "Cobra" and the Cobra logo are registered trademarks for Ford Motor Co., Inc. clubcobra.com forum members agree not to post any copyrighted material unless the copyrighted material is owned by you. Although we do not and cannot review the messages posted and are not responsible for the content of any of these messages, we reserve the right to delete any message for any reason whatsoever. You remain solely responsible for the content of your messages, and you agree to indemnify and hold us harmless with respect to any claim based upon transmission of your message(s). Thank you for visiting clubcobra.com. For full policy documentation refer to the following link: CC Policy
Links monetized by VigLink